Continental XO-1430 Development
Part 2: 1932 and 1933
by Kimble D. McCutcheon
Published 3 Aug 2025; Revised 15 Aug 2025
| Part 1: Introduction and Background | Part 2: 1932 and 1933 |
| Part 3: 1 Jan 1934 to 30 Jun 1934 | Part 4: 1 Jul 1934 to 31 Dec 1934 |
| Part 5: 1 Jan 1935 to 30 Jun 1935 | Part 6: 1 Jul 1935 to 31 Dec 1935 |
| Part 7: 1 Jan 1936 to 30 Jun 1936 | Part 8: 1 Jul 1936 to 31 Dec 1936 |
| Part 9: 1 Jan 1937 to 30 Jun 1937 | Part 10: 1 Jul 1937 to 31 Dec 1937 |
| Part 11: 1938 | Part 12: 1 Jan 1939 to 30 Jun 1939 |
| Part 13: 1 Jul 1939 to 31 Dec 1939 | Part 14: 1940 and Conclusion |
| Notes to Readers | XO-1430 People | Glossary |
16 Dec 1932. Materiel Command Power Plant Laboratory civilian engineer Ford L. Prescott issued Engineering Section Memorandum Report No. E-57-126, "Continental Single-Cylinder Poppet Valve Engine (Progress Report), which concluded that it was possible to design a poppet valve cylinder for high output. Prescott thought that high supercharger boost was undesirable since the supercharger design problem was so difficult that the resulting efficiency would probably be lower than could be obtained with a larger displacement engine of moderate performance. He analyzed the 1,000 hp, 1,008 in³ displacement engine using 12 Hyper No. 1 cylinders for weight and determined it would weigh about 1,000 lb, excluding cooling system and turbosupercharger.
Prescott recommended continued cylinder design studies to fine the lightest cylinder form for moderate ground boosting, and also suggested other engine arrangements should be analyzed to find the most desirable type for development. A cylinder designed along the lines of the Allison high-output cylinder was being tested by the PPL and had proven capable of operation at 3,000 rpm and 419 psi bmep with 48.2 inHgG boost. Continental had begun testing its Hyper No. 1 cylinder. He remarked that the weight analysis of the 1,008 in³ 12-cylinder engine was very disappointing, since the bare engine with geared supercharger would weight in excess of 1,000 lb; this heaviness was largely due use of separate cylinders designed for high specific output. He pointed out that European designs had achieved good specific weights using larger-displacement instead of high-output cylinders. Several options were being analyzed, including a 12-cylinder hex engine using high output cylinders, a built-up steel cylinder and a dry-liner aluminum cylinder.[USNARA RG 342 RD1670, 502-2-108 O-1430 to 340630. 3-4a]
6 Feb 1933. Continental Chief Experimental Engineer R.N. DuBois released "Report of Performance and Endurance Test of Continental 'Hyper' Engine No. 1." The object of this test was to obtain information on the performance and endurance of the engine at high output with Prestone cooling. In summary, the engine developed 310 psi bmep at 2,200 rpm, 250°F jacket temperature, 60°F carburetor air temperature and 30 inHgA boost. At 3,000 rpm it achieved 279 psi bmep. An endurance run at 3,000 rpm, 255 psi bmep and 0.54 lb/bhp/hr brake specific fuel consumption (bsfc) using 24 inHgA boost had begun and 8 hrs had been run by the time the report was released. The first few hours of this run indicated that the cylinder was not getting enough oil and that the piston clearance was low. A squirt hole was drilled in the connecting rod lower end and the piston clearance increased from 0.022" to 0.030". The aluminum alloy rocker box casting failed at 8 hrs because the rocker shaft boss section was insufficient to withstand the 200 lb valve spring loading at 3,000 rpm.
DuBois concluded the cylinder performance was satisfactory; no fundamental defect had appeared during the operating 87 hrs. The Lo-Ex (a low-expansion aluminum alloy) piston did not show the expected bearing qualities and work was indicated on land clearance and top land width to avoid ring sticking and wear. DuBois recommended the endurance run be continued to 25 hrs, using a new rocker box casting and 160 lb valve springs, which had given no previous trouble.
Description
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| Hyper Cylinder |
Hyper cylinder No. 1 design featured a 4.625" bore, 5.000" stroke and 84.001 in³ displacement. Its forged carbon steel barrel was screwed and shrunk into a cast heat-treated head of modified Y-alloy with a separate hardened SAE #2340 steel water jacket shrunk over the barrel and head shoulder. The liquid space around the barrel was joined to the head jacket by two flanged connections fastened by studs and nuts. The enclosed single overhead intake and exhaust valves, both sodium-cooled, were operated through rockers from a central camshaft with hollow-faced, large-nose-radius cams. The rockers had rollers at both the valve and cam ends with clearance adjustment at the valve. The valves ran in aluminum bronze guides inclined at 35° to the cylinder axis. The valve seat inserts were cast from a special aluminum bronze, and the exhaust seat was faced with Stellite. The BG 157 spark plugs were inclined 50° to the cylinder axis and were retained in aluminum bronze inserts, screwed and pinned in opposite sides of the head at a 65° angle to the valve plane. The forged Lo-Ex piston had four transverse rubs under its head, three compression rings and two oil rings with vented grooves, one above the piston pin and one at the skirt bottom. All rings were 0.125" wide. The oil hardened, Timken-axle, chrome-nickel-molybdenum steel full-floating piston pin used chill-cast Y-alloy end plugs. Compression ratios of 5.0:1, 5.5:1 and 6.0:1 could be obtained with various spacer and piston combinations. Valve timing was as follows: intake opened at 20°BTC; exhaust closed at 20° ATC; intake closed at 55° ABC; exhaust opened at 65° BBC.
Method of Test
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| P02Fig001. Test Setup | |
The engine was connected to a General Electric Type TL C-20 dynamometer with a beam scale. Fuel was measured by volume in a calibrated tank; an orifice flowmeter was used for preliminary tests. Air consumption was measured by a sharp-edged orifice in the high pressure air line. Figure 1 shows the test setup. A well-type mercury manometer indicated the carburetor tank pressure. Carburetor air, cylinder and air-metering orifice temperatures were obtained with iron-constantan thermocouples. Oil and coolant temperatures were indicated by "Motometer" vapor-pressure thermometers, and the coolant outlet temperature was measured by a mercury thermometer. A "temperature plug" similar to that used by the USAAC to detect detonation was installed. When indicator cards were desired, a "Farnboro" electric indicator with special Continental disc valve was used and was driven by the engine crankshaft.
All results were corrected to an atmospheric pressure of 29.92 inHgA and carburetor entrance temperature of 60°F; no humidity correction was used. After running-in and subsequent inspection, a run was made to 3,025 rpm, using a neon stroboscope for valve spring and rocker observation. The valve operation was regular and no bounce was seen up to 3,025 rpm. The springs, which were 160 lb tension, were surging sufficiently to mark adjacent coils. Above 2,800 rpm an intermittent clatter was noticed. A 5 hr run, unsupercharged, at 2,800 to 2,900 rpm was run, after which a teardown inspection showed the condition to be satisfactory. On rebuilding, the piston was changed in order to increase the compression ratio from 5.5:1 to 6.3:1 and the 160 lb valve springs were replaced with 200 lb springs.
Runs form 2,000 to 3,000 rpm at 10, 20 and 30 inHgA carburetor intake pressure were made, with results shown in Figure 2; at 30 inHgA and 2,300 rpm the single cylinder produced 75.4 bhp (12-cylinder total = ~905 bhp). The volumetric efficiency and spark advance were shown in Figure 3, the volumetric efficiency being corrected for the compression of the residuals to the supercharger pressure. The volumetric efficiency was quite high and unchanged by supercharger pressure variations. The flat output curve at 30 inHgA boost has not been explained, although from spark advance curve examination it appears the engine is over compressed at the 6.5:1 compression ratio and 30 inHgA boost; and with better fuel the 30 inHgA output curve will show a distinct peak at 2,200 rpm as in the curve at 10 inHgA and 20 inHgA boost, Figure 4 shows the jacket outlet and cylinder temperatures for the same group of runs. The cylinder temperatures were taken just below the spark plug on the cylinder intake side. The curves show the cylinder temperature to be practically independent of boost or speed, so long as the jacket temperature was maintained constant.
Figure 5 is cross-plotted from Figure 2, showing output versus boost at 2,200, 2,500, 2,700 and 3,000 rpm. Figure 6 shows a power curve using for each speed the maximum boost possible at 2,000 rpm without detonation, at fuel consumption at approximately 0.53 lb/hp/hr. Detonation was quite difficult to detect on this engine and a temperature plug was inserted after a piston had been melted through by undetected detonation with excessive spark advance at 30 inHgA boost. Figure 7 shows friction mean effective pressure at 2,000, 2,500 and 2,000 rpm.
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| P02Fig002 | P02Fig003 | P02Fig004 | P02Fig005 | P02Fig006 | P02Fig007 |
Run Logs
[DuBois, R.N. Report of Performance and Endurance Test of Continental "Hyper" Engine No. 1 (Detroit, Michigan: Continental Aircraft Engine Co.) 6 Feb 1933.]
10 Apr 1933. Continental Vice President and General Manager Ray S. Deering wrote PPL civilian engineer Robert Insley informing him that Continental Chief Engineer Norman. N. Tilley had requested a cost estimate for an additional Hyper Cylinder. This item was essentially a duplicate of the two Continental had already produced for the USAAC, except that the head and barrel coolant jackets were to be smaller. Only the bare cylinder studding assembly, with coolant connections, studs, valve seats and guides was to be supplied. The engineering, core box changes, materials, purchased finished parts, labor and shop overhead would cost 986.94; no administrative overhead was included, as the USAAC was anxious to begin testing.[10 Apr 1933 letter, Deering to Insley, author's collection.]
[30 Jun 1933 letter, Long to MatCmd, author's collection.]
26 Jul 1933. Acting Aircraft Branch Chief Capt H.Z. Bogert issued Memorandum Report AD-51-126 Addendum 1, reporting on a study of XO-1430 mounting. The engine appeared to be easily adaptable for wing mounting as shown on drawing S34X17 (not found). The engine and its cowling to provide satisfactory accessibility required a leading edge notch about 80" deep, with the front spar aft 20% of the 150" wing chord and the propeller 33% ahead of the leading edge. If nose box-beam wing construction with the rear face at approximately 30% chord was contemplated, a new structural problem would arise, but it might be possible to provide strength and rigidity by building a box of equivalent strength aft of the nose box spar. Another installation study was to be made with a two-stage supercharger.[USNARA RG342 RD1670, 502-2-108 O-1430 to 340630. 8]
5 Aug 1933. USAAC Procurement Section Chief Maj H.A. Strauss wrote Continental regarding the 1,000 hp, 1,425 in³ displacement opposed type engine.
1. The following proposal for continuing work on the high-speed, 12-cylinder, opposed type, liquid-cooled engine is submitted for your consideration and comment. The work to date has been in the form of single-cylinder testing and design studies to determine the feasibility of a 1,000 hp opposed engine type and to determine whether a cylinder could be developed that would permit obtaining 1,000 hp at 3,000 rpm with a displacement of 1,425 in³ The USAAC has closely followed the cylinder design and testing and the multi-cylinder engine design studies. This project has now reached the point where it is desired that your company accept full and complete responsibility for the design, construction and test of the multi-cylinder engine, with the USAC acting only in an advisory capacity. If the Continental Aircraft Engine Company is interested in undertaking this development, it is desired that estimates of costs be furnished on each of the following phases with a breakdown of the quotation at several logical points in each phase. In making these estimates the following project divisions should be observed:
Second Phase (B) The contractor will construct a 12-cylinder engine in accordance with the drawings and requirements covered by the first phase. This engine will have a General Electric designed geared supercharger, which will be furnished by the contractor.
Third Phase (C) The Contractor will conduct a development test in accordance with the current issue of Air Corps Specification 28144, at an actual horsepower of not less than 1,000 and at a speed not less than 2,800 rpm.
3. The Government will cooperate, as far as practicable, in the inspection and advice concerning the engine or engine parts during the process of fabrication and/or construction. Inspection personnel will act in an advisory capacity only and will not be authorized to reject material or fabricated parts; they, however, will call to the attention of the contractor for his consideration, such materials as are not in accordance with U.S. Army Specifications, unsatisfactory workmanship, and practices and processes not in accordance with Government standard requirements.
4. It is further requested that an estimate of the time required to complete each of the three phases, or parts thereof on which quotations are submitted.
18 Aug 1933. Engineering Section Chief Maj C.W. Howard wrote Continental regarding their letters of 26 and 27 Jul 1933 regarding Purchase Order 33-3804 – Endurance Test of Hyper Cylinder No. 2. In their letters, Continental had mentioned using a solid exhaust pipe connected to the cylinder flange and subsequent breakage of cylinder flanges and studs during endurance running. The Engineering Section had encountered poor results with solid exhaust pipe connections, suggested that the cylinder failure at 49.95 hrs may have resulted from the solid pipe, and that future running should employ a more flexible arrangement. While flexible tubing had also been unsatisfactory, short exhaust stacks that telescoped into another pipe had worked well. The stack entered the pipe at about 3" and the joint was covered by a woven asbestos tape that was wired in place. A boss welded to the exhaust stack near the flange and a small jet of water was injected into the exhaust stack after the engine was running.[18 Aug 1933 letter, Howard to Continental, author's collection.]
These figures were all based on 950 fps propeller tip velocity. This study indicated that three propeller reduction ratios (5:3, 2:1 and 5:2) should be designed. N.N. Tilley questioned whether a spacer should be used between the propeller cone and thrust nut; the Propeller Unit thought this necessary because of the different hub lengths of fixed- and controllable-pitch propellers. The Installations Unit opined that coarse screens should not be used in the oil pump oil-in lines because they would restrict cold oil flow; such screens were desirable in the oil scavenging system.[USNARA RG342 RD1670, 502-2-108 O-1430 to 340630. 9]
9 Sep 1933. Ford Prescott released Memorandum Report E-57-126 (Again! They needed to assign unique report serial numbers!) covering a conference at Wright Field on 22 Aug 1933 on the 1,000 hp Engine attended by R.L. Long, N.N. Tilley and C.N. Furay of Continental and Division representatives. (NOTE: Although the release date is out of order, the subject matter belongs here. Also, this conference was an obvious prelude to the larger 5.500" bore, 5.000" stroke, 118.75 in³ displacement (1,426.5 in³ 12-cylinder) Hyper No. 2 cylinder.)
The engine's weight was discussed, including the impact of the proposed long nose, gun and tachometer drives. Chenoweth stated that the total weight must not exceed 1,120 lb, which, allowing 0.28 lb/hp for the cooling system, a 1,400 lb installed weight; this was intended to be competitive with air-cooled installations. The calibration and endurance tests should include reduction gearing as these gearing losses were undetermined. Cams for single-cylinder testing of the new setup were left to Continental's discretion. Tilley proposed to check whether the oil jet directed at the piston crown was really necessary since the multi-cylinder engine with its larger and less restrictive bearings would throw more oil. Detailed test requirements were tabled for a later date to allow discussion of other points that needed immediate attention. Continental thought the front gun synchronizer drive would unnecessarily complicate the engine and increase its weight; only the rear synchronizer drive would be included. The interference of the electric tachometer solenoid with the second tachometer drive was deemed unimportant since a mechanical tachometer would not be used with the electrical type on the same engine. Continental was to select the Cuno oil filter size in concert with the manufacturer. Continental's objections to 1" pipe threads for oil connections were overruled because they had provided good service. Oil packing on the tachometer drives was mandatory as this would prevent oil from seeping through the flexible shaft and into the tachometer.
The desired 2" diameter x 2.25" high space for shielded spark plugs was deemed impossible, since the cylinders had been designed to accommodate the BG and MT high-tension shielded plugs originally specified for the cylinder. The longest spark plug lead was about 60", which meant that Packard shielded cable was acceptable; it was agreed that laboratory tests would be made before a final decision. There was considerable discussion about whether the Scintilla double magneto could be reversed in the field and about various schemes to do so; no conclusion was reached. A type F-6 fuel pump driven at propeller speed was indicated and had a 300 gph flow at 1,700 rpm.
Continental objected to proposed standard vacuum pump drive because the small shear member might give trouble in the winter when oil was viscous (this was before dry-air pumps). The USAAC had based large procurements on pumps with standard drives and desired to stick with that design. Continental's main objection was the mounting pad height required by the wet pump drive member.
The team decided to lay out a bevel gear drive from an exhaust-driven turbine through a vertical shaft to be a modified blower mounted on the engine rear. This would probably call for a special blower in view of the need for an intercooler between the blower and engine. The weight would be increased over a combined turbine and blower mounted below the engine, since in this case the geared blower would be omitted from the engine, and the drive from turbine to blower would be lighter and simpler. Objections arose to the experimental nature of the high-speed bevel gear drives, along with removal of blower inertia fro the accessory drives at the crankshaft rear, a condition that would impose severe torsional stresses on the magneto, generator and fuel pump drives. The present drive was through a spring coupling like those used in radial engines that would not function without the supercharger inertia load.
A question arose over payment for the 50-hr test that had terminated at 49.05 hrs. Lt Powers stated that the only settlement possible under the circumstances was for Continental to invoice the USAAC for 49.0833 / 50 of the amount agreed for this test. Long pointed out that 11 hrs had previously been run on Cylinder No. 1, but Lt Powers stated that this could not be taken into consideration under existing regulations.
Continental wondered whether the USAAC would consider a cost-plus basis for construction of the 12-cylinder engine, in view of the necessity of covering unforeseen contingencies in an experimental contract; this topic was tabled for later discussion. Continental also objected to the minutely detailed specification, but it was pointed out that these removed uncertainties, basing estimates on definite requirements.[USNARA RG342 RD1670, 502-2-108 O-1430 to 340630. 11 – 013]
19 Sep 1933. Continental responded to the USAAC's 5 Aug 1933 1,000 hp, 1,425 in³ displacement opposed type engine specification with a letter proposal from Sales Manager Ray Long to MatCmd. Apparently there had been two conferences regarding this on7 and 16 Sep 1933. Following up on suggestions made during the conferences, Long recommended that the project be divided into four major phases, each with subdivisions as applicable.
Phase No. 2 was the completion of detail and assembly drawings, bills of material and parts lists of the 1,000 hp 12-cylinder opposed liquid-cooled geared engine, of which one set of Vandykes was to be furnished to the Government. This engine design was to meet the requirements of the 5 Aug 1933 letter, with certain alterations and additions already discussed and agreed upon between Continental and USAAC engineers. This phase was priced at $16,770.17.
Continental estimated that Phases 1 and 2 could be completed in 180 calendar days from the date of contract. To further expedite progress, Continental had already released the necessary pattern changes and proposed to carry on without further delay in advance of formal USAAC authority.
Long estimated that Phase 3 could be completed within 130 calendar days after starting work thereon. He estimated 100 days if only Sections a and b were authorized. Phase No. 3 could be started within 60 days of Phase 2 start.
Phase No. 4 covered development test in accordance with the current issue of Air Corps Specification No. 28144, at an actual output of not less than 1,000 hp and a speed of not less than 2,800 rpm.
In view of the UASSC's inability to commit at that time to the Phase No. 4, Long did not submit pricing, but voiced Continental's willingness to complete the project on a cost no-profit basis if and when USAAC was in the position to authorize such work.
Payment for each Phase and/or Section was to be made upon completion and acceptance thereof and was not to be contingent upon the completion or acceptance of any other Phase or Section. In view of the fact that the prices were based on conditions at the time of quote, long reserved the right to revise any portion of the quotation on which formal inquiry was not received from the Government within 30 days from date. However, it was understood that any change in quotation was to be based on later material and labor fluctuation from then-current costs at the time of acceptance. [19 Sep 1933 letter, Long to MatCmd, author's collection.]