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R-4360 Service History
C-97 and KC-97 Aircraft in Air National Guard Units
Submitted by John Schauer
MINNESOTA AIR NATIONAL GUARD
133D MILITARY AIRLIFT GROUP (MAC)
Minneapolis-St. Paul Int’l Aprt
St. Paul, Minnesota 55111
(Mid-1966??)
REPLY TO ATTN OF: GCMD
SUBJECT: Maintenance
TO: Pilots and Flight Engineers
1. So
many years have gone by since I have had the opportunity to write a letter to
aircrews that I do not know if I can revive the nasty side of myself
sufficiently to make an impression. As a fresh start maybe I should confine this
letter to some information which will be of interest to you if you have interest
at all.
2.
This message will be restricted to R4360-59B engines. Out of 17 Air
National Guard bases that fly C-97G’s, we rank 16th in engine life.
That really isn’t news to you but I thought I would let you know things really
haven’t changed much. The unit which ranks first over the past year average over
400 hours more time on their engines.
3.
The average overhaul cost on one of our engines is $21,125 which includes
both parts and labor. It may surprise you to learn that the Air Force is still
making improvements on the R4360-59B. There have been eleven recent improvements
made which I will briefly describe for you.
I.
Master rod Bearing Lubrication – deactivation of the oil
diverter-segregator valve and modification of the oil tank.
II.
Master rod Bearing Improvements – reduction of silver on the bearing
back to prevent flowing of the silver and buildup of high spots on the inside
diameter.
III.
Front Main Bearing Lubrication – planetary magneto drive oil feed
passage increased from 0.030 inch to 0.060 inch, metering oil jet to front cam
removed, pressure oil skates incorporated in the planetary magneto drive gear,
front main bearing removed and re-lead indium plate at each overhaul.
IV. Exhaust valve seat pinch fit increased – a slight increase in the pinch
fit between the cylinder head and exhaust valve seat plus an improved
technique in sizing of the seat recess.
V.
Exhaust manifold front anchoring neck replacement – incorporation of a
doubler patch and installation of a new neck manufacture from AMS-347
stainless steel.
VI.
Exhaust manifold outlet – a replacement flange manufactured from
AMS-347 stainless steel is machine welded in place.
VII.
Pushrod cover seal material – a new Fluorocarbon Rubber seal (white in
appearance) is now being used.
VIII.
Exhaust valve guide sizing – exhaust valve guides are being honed
instead of reamed to get a more accurate size.
IX.
Valve tappet roller pins – because of increased engine life (?) it has
been necessary to increase the silver thickness on the tappet roller pins to
reduce possible failure.
X.
Cracked collector case engine mount pads – revised maintenance
instruction for dynafocal mount installation which includes a higher torque
setting during build-up. Just in case you run into this problem out in the
system, we can now continue an engine in service with one mount cracked
provided the crack has not progressed downward off the pad portion of the
case. The attaching screws on the cracked mount and adjacent mounts will be
removed one at a time, lubricated, reinstalled, and the screw heads will be
painted with yellow paint. You would never find one anyway.
XI.
Spark plugs – two new plugs have been approved for our use. They are
the Champion 7P71 and the Auto-lite PL350. They are fine wire and have the
same rating as the AC-281. Now all we have to do is get some.
4.
There are also eight more improvements under study at this time with test
engines being positioned at various bases.
I.
Increased Cylinder Wall Lubrication
Air Force has modified one R4360-59B engine to
increase the oil supply to the cylinder walls in an effort to improve piston
reliability. This engine was operated at 60 inch manifold pressure 2,700 RPM
for 25 hours. Engine was disassembled and pistons were found in excellent
condition. This engine was reassembled tested and identified as a service test
engine. R4360-59B engine P514966 was shipped to Wilmington, Delware and SAAMA
message SANTTA 91511, 16 Mar 66, advises activity of required reporting.
II.
Chrome Plated Piston Ring in Second Groove
During inspection of engines at teardown it
was noted that in some instances the second compression ring had lost its
tension. Although no incipient piston failures were found, there was evidence
of increased blow-by and high ring friction. In an effort to correct this
unsatisfactory condition, one R4360-59B engine P515811 has satisfactorily
completed testing with chrome plated piston rings in the second compression
groove in all 28 locations. This engine has been shipped to Nashville, Tennessee
as a service test engine. In view of the favorable test results 10 additional
engines are being built to accelerate evaluation. Activities receiving these
engines will be advised.
III. Piston
Anti-Friction and Insulating Coatings
A new anti-friction coating was developed by
the manufacturers Materials Development Laboratory for use on piston walls.
This coating consisted of molybdenum disulfide and lead oxide in an epoxy
carrier, which is impervious to oil. One single engine cylinder has completed
endurance test. Additional testing is being developed.
An insulating coating was applied to the dome
of an R-2800 engine piston to retard the flow of heat to the piston thereby
allowing the piston to retain its physical properties for longer periods. This
piston has completed 19 hours running on a single cylinder engine. Presently a
coated piston is being prepared with temperature measuring equipment to
evaluate true effects of the dome coating.
IV. The engine manufacturer is continuing to
investigate new alloys which could be used to increase service life and offer
relief for troubles associated with operational environment. Pistons of a new
higher strength alloy were fabricated and tested. Initial tests were conducted
at high overload conditions of 67 inch manifold pressure and 2,800 RPM, ring
problems usually experienced at these extreme gas pressures were encountered,
but were not transmitted to the pistons. Slight dimensional modifications are
being made to accommodate the piston for the improved high temperature
strength properties and the differences in coefficient of expansion.
Fifty-seven pistons have been delivered to five Airlines for field evaluation.
(R-2800 Engines)
V. Starter
Drive Seal
Air Force engineering and the engine
manufacturer were furnished seals known to be leaking. Sectioning of the parts
showed in each instance that the sealing diaphragm had become brittle and
fractured. After consideration and testing of several new seals, decision was
made by engineering to retain the present seal and install a diaphragm of more
durable material which will not deteriorate at temperatures in the vicinity of
200° F.
VI.
Spinning Intake Valves
Laboratory testing has been conducted at SAAMA
during the past several years to determine cause and corrective action to
prevent rapid spinning of the intake valve which occurs at high power. By
positive locking lower valve spring washer accelerated valve rotation was
stopped in laboratory engine. To obtain service evaluation R4360-59B, P517245
and P516849 were modified and shipped as service test engines to Will Rogers
APRT Okla. SAAMA message SANTTA 91519, 22 Mar 66, advises activity of required
reporting.
VII.
Engine Balance
During recent discussions concerning R-4360
engine reliability the question of engine balance was brought up. Activity at
Savannah Georgia has requested they be furnished four known balanced engines to
service evaluate. Since a number of known changes have been made in design and
repair which could have changed balance to some extent, Air Force engineering
and the manufacturer were requested to determine if this engine is still
adequately balanced. The engine manufacturer advises that the R4360-59B engine
configuration relative to 64.10-lb crankshaft balance weight and finds
current parts are completely satisfactory with no design or balance
modifications required. Preliminary calculations by Air Force engineering
shows no changes in part configuration required. Arrangements have been made
to have contractor accomplish measurement of actual weight of various
configuration rotating mass to confirm calculated findings. Target date for
assembly of four known balanced engines is August 1966.
VIII.
Test of Self-lubricating Cam Follower on R-4360 Magneto Breaker
A breaker with a self-lubricating cam follower
has been developed which eliminates the lubricating felt. SAAMA is presently
performing a block test (400 hours) to determine if the self-lubricating cam
follower is superior to the present breaker. Upon completion of this run, it
will be installed on a test block engine having a history of magneto problems
and run for 150-400 hours. Target date of completion, 1 Aug 1966.
5.
There were several discussion items of interest and I have picked out
three which are of interest to you. The subjects are exactly as presented. I
realize this is getting to be a long letter which may discourage you from
reading it at all but I also think it is information you should have.
I.
The Cause and Correction of Exhaust Valve Seat Failures
A.
This discussion will include basic principles of operation of valve and
seat, types of failures, procedures at overhaul, changes in engine operation
techniques necessary to obtain consistent cylinder reliability. This discussion
will not include in detail abnormal causes of failure such as overspeeding or
overboosting the engine beyond design limits and cracked or otherwise faulty
parts. Temperature will be the key word throughout the discussion. The complete
story of operation is presented in order that all personnel concerned can better
understand all the overlapping phases of design, operation, type of failures,
manufacturing, overhaul and operational technique necessary to insure reasonable
cylinder life on any Reciprocating Aircraft engine.
B.
The exhaust flame directly affects the valve, seat and cylinder; hence it
is necessary to understand the effect of engine power, speed, and fuel air
mixture on exhaust flame temperature before we can understand the complete
operation of the valve seat. Starting at idle speed, the exhaust temperature
rises rapidly with increased speeds until maximum cruise power is reached at
which time the power enrichment valve starts to open which sharply reduces the
actual flame temperature. Cylinder head temperature continues to increase at
engine speeds above maximum cruise due to the increasing number of power
impulses. Above maximum cruise the cylinder head has reached its basic maximum
capacity to cool; and therefore, the amount of fuel is substantially increased
as a combustion coolant to compensate for the cylinder cooling deficiency. Since
use of added fuel over and beyond that normally used would reduce power
excessively and since cylinders will operate satisfactorily under power at
temperatures above those obtained at maximum cruise, a compromise between
cylinder head temperature and power is used to give the best overall results.
C.
The exhaust valve head is exposed to combustion temperatures during the
power stroke and the entire head of the valve and part of the valve stem is
exposed to exhaust temperature during the entire exhaust stroke; hence the valve
is exposed either partially or completely to high temperature (1,800-2,600°F) for
approximately 440° of crankshaft travel. Therefore, the valve is exposed either
partially or completely to extreme heat approximately 37 seconds out of each
minute. The valve dissipates this heat through the valve guide and through the
seat where the two faces contact.
D.
The ni-chrome steel exhaust valve seat used in Pratt & Whitney R-4360
engines is installed in the seat recess with a 0.0058-0.0073" pinch fit. This is
accomplished by cutting the recess to a specific size, gaging and obtaining
premeasured seat of a known size which will provide the required fit. The
cylinder is then heated to around 500°F and chilling the valve seat to less than
10°F by use of dry ice. When the seat and seat recess are stabilized at room
temperature, the seat is then between 0.0058-0.0073" tight. Ni-chrome R-4360 exhaust
valve seat has a measured expansion rate of 0.0000045 per inch unit length for
each degree Fahrenheit change. Aluminum has an average expansion rate of
0.000001234 per inch unit length for each degree Fahrenheit change. For example a
2.800" diameter valve seat and a 2.793" seat recess were elevated to 600°F;
the 0.007" pinch fit is reduced to 0.0046" loose.
VALVE SEAT 0.0000045 X 2.800 X (600°-70°) =
0.00667
SEAT RECESS 0.000001234 X 2.793 X (600°-70°) =
0.0182
SEAT RECESS 2.793 + 0.0182 = 2.8112
VALVE SEAT 2.800 + 0.0066 = 2.8066
_______
VALVE SEAT LOOSE = 0.0046
When the cylinder is cold (70°F) and the engine
is started the seat temperature rises first and to a considerable higher
temperature than the seat recess. Hence, after ½ minute of operation, the seat
temperature is about 600°F and the seat recess temperature is around 200°F, the
pinch fit will have changed from 0.007" to 0.0099" pinch fit. Now the
compressibility of aluminum is such that a maximum pinch fit of 0.007" is about
all that will be retained, as the seat recess would be compressed approximately
0.0029" and would reduce the pinch fit under these temperatures of (600°F and
200°F) back to 0.007 inch. This, in turn, would reduce the pinch fit with a cold
cylinder from the original 0.007" down to about 0.0049" pinch.
E.
With the fundamentals now covered, it should be readily evident that the
exhaust valve seat is retained in a hot engine by combustion heat saturated up
by the valve seat itself and the valve. Take this heat away suddenly and you
have a loose valve seat. The first several times a cylinder is exposed to this
condition, it will probably do little damage because of a retaining lip designed
into the seat specifically for this purpose. This locking device does not keep
the seat tight; its only function is to retain a loose seat. Mechanical
operation of the valve mechanism with a loose seat will eventually pound the
seat into the cylinder head, upsetting valve clearance which in turn aggravates
the pounding by the valve. This can then only result in the seat coming
completely loose from the cylinder or total cylinder failure.
F.
At this point it might be said “JUST FOLLOW THE NORMAL OPERATING
INSTRUCTIONS IN THE AIRCRAFT OPERATING MANUAL” and you will have reasonable
cylinder reliability. But some time must be spent discussing the specific
condition known to induce cylinder problems:
1.
Fast engine starts – The colder the weather the more detrimental – Keep
engine RPM down until engine is warm.
2.
Operation of engine less cowling – This should be avoided, except for
short period oil leak check – RPM less than 1,200, CHT 160°C MAX, 2 minutes
maximum.
3.
In flight shutdowns – Not recommended, except in actual emergency.
4.
In flight power reduction – Should be gradual – Never pull power off to
idle when CHT exceeds 200°C, except in emergency.
5.
Deterioration of the ignition system in service can be a major problem to
cylinder life. Cylinders misfiring causes rapid cooling of the exhaust valve
seat. This can result in a loose seat condition and will eventually cause seat
failure. Malfunctioning engines should only be operated under emergency
conditions.
6.
Propeller thrust reversing – Should only be used when necessary – Causes
high cylinder head temperatures and is always followed by low power (idle
operation).
7.
Engine shutdown – Must be below 180°C CHT – if this is impossible – Rotate
engine several seconds with starter if possible.
8.
Cooling Hood baffles – Must be latched and in good condition – always
replace or repair defective hoods.
II.
MIL-L-22851 Oil vs. MIL-L-6082
In 1964 an investigation was conducted to
determine the cause of engine problems being experienced with MIL-L-6082 oil
with two percent (2%) cyclohexanone. Inspection of the general internal
condition of reciprocating engines repeatedly singled an abnormal build-up of
sludge, carbon, and lacquer in Air Force engines. Field replacement of nose
sections, magneto spacer cases, and blower clutches were at an all time high.
Erratic torque, sluggish propellers, etc. were all too frequently reported.
In view of the above, an intensive investigation
was conducted by SAAMA to find an improved lubricant for Air Force engines. Our
findings were:
A.
An ashless dispersant oil (MIL-L-22851) was developed in co-operation
with aircraft manufactures including Pratt & Whitney, Wright Aeronautical,
Lycoming, and Continental Motors. All engine manufactures and FAA sanction the
use of this oil.
B.
The lubrication and heat transfer capabilities of MIL-L-6082 oil and
MIL-L-22851A oil are identical. The base stock oil utilized to produce
MIL-L-22851A Type II oil is MIL-L-6082 Grade 1100 Oil. The only difference being
the additive as depicted in paragraphs 3.2.1 through 3.2.2 of Military
Specification
MIL-L-22851A.
C.
Navy and Army have converted to MIL-L-22851A oil. Navy has been utilizing
MIL-L-22851A oil in all their aircraft since 1961.
D.
As of January 1962, 72 commercial users world-wide, have converted to
ashless dispersant type oil.
E.
Special oil qualifications tests have been conducted by SAAMA, MAAMA,
AFAPL, Navy, and contractors to insure oil delivered to the Air Force meets
requirements set forth in Military Specification MIL-L-22851A. Tests will be
conducted to insure quality of oil does meet specification limits.
F.
SAAMA has a program in effect since mid 1964 to evaluate results of
MIL-L-22851A oil. Approximately five (5) different engine models are given
special teardown analysis at SAAMA each month to evaluate effects of
MIL-L-22851A oil. Internal parts of engines are inspected for condition of
bearings, wear points, cleanness, if oil passages are free of foreign matter,
etc. Analysis of results has provided conclusive proof MIL-L-22851A oil is
satisfactory for use in all Air Force reciprocating engines.
Availability of MIL-L-22851A Oil
MIL-L-22851A type oil is available throughout
the Air Force except in USAFE and Spain. Spain and USAFE should deplete their
stock of MIL-L-6082 oil by 1 Oct 1966. Rhein-Main AB has a supply MIL-L-22851A
oil on hand to service aircraft from outside the theater that have converted.
Aircraft that have converted and make stops at other bases in that theater can
intermix (Make-up oil) MIL-L-6082 oil with MIL-L-22851A oil. However, the use of
MIL-L-6082 oil as make-up oil will reduce the dispersant action of MIL-L-22851A
oil, percentage wise, depending on amount added.
III.
Engine Oil System Maintenance
Recommendations have been made to OCAMA
decreasing the frequency for oil screen cleaning intervals. Upon compliance with
T.O. 1C-97-627 and when the engine has operated 200 hours or more on
MIL-L-22851A oil, the following inspection and maintenance requirements are
recommended.
A.
Clean and inspect main oil screen each 50 hours on KC-97 A/C and each 100
hours on C-97 A/C.
B.
Drain engine sumps, oil coolers and main oil tanks each 200 hours.
C.
Under special inspections:
1.
When main oil screen is found more than 35% clogged with carbon drain
engine sumps, oil coolers and main oil tank; then repeat oil screen cleaning
after each flight until screen is clean.
2.
Drain main oil tank sumps when engines have not been operated for 24
hours.
6.
This teardown deficiency report information along with some reports on
our engines which have been sent back for depot repair during the past few
months will give you some indication of what has happened to us compared to the
big picture.
7.
We really aren’t as bad as we may look. January through March 1966 our
engine life was up enough to put us in 10th. place instead of 16th.,
and I hope it keeps improving. This has been so long that I am too tired to be
nasty so it will have to wait until next time.
MARVIN A. THORSEN
LtCol, MinnANG
Commander
R-4360-59B C/KC-97
TEARDOWN DEFICIENCY REPORT (TDF) SUMMARY
PURPOSE: This report contains TDF data by primary reason for overhaul and
compares the previous years data.
|
Reason for Overhaul |
Percentage
Jun-Dec 1965
(C-97 ANG ENGINES ONLY) |
Percentage
1964 |
Percentage
1963 |
Percentage
1962 |
Percentage
1961 |
|
Maximum Time & Directed |
31.0 |
9.1 |
18.6 |
31.8 |
32.5 |
|
Master Rod Bearing Failure |
13.4 |
30.6 |
22.6 |
12.8 |
10.3 |
|
Burned Piston |
13.4 |
12.2 |
7.3 |
4.5 |
9.2 |
|
No Failure Found |
12.0 |
2.0 |
7.2 |
4.7 |
6.1 |
|
Turbo Supercharger Failure |
2.1 |
3.0 |
2.8 |
1.3 |
3.6 |
|
Collector Case Cracked. Engine Mount Pad |
3.5 |
4.0 |
2.7 |
2.3 |
1.7 |
|
Overboost |
1.4 |
1.0 |
2.3 |
3.4 |
3.9 |
|
Foreign Object Damage |
1.4 |
11.2 |
2.2 |
11.2 |
5.1 |
|
Hydraulic lock |
1.4 |
2.0 |
1.9 |
3.0 |
2.4 |
|
Exhaust system front anchoring neck failure |
2.1 |
1.0 |
1.0 |
1.2 |
|
|
Exhaust valve seat loose |
0.0 |
1.0 |
0.9 |
2.7 |
0.4 |
R-4360-59B Engines C-97 Aircraft
TEARDOWN REPORT FINDINGS SUMMARY
June – Dec 1965
|
Reason for Teardown |
Number |
142 (ANG) Engines Percent |
|
Maximum Time |
44 |
31.0 |
|
Master Rod Bearing
Failure |
19 |
13.4 |
|
Piston Burned |
19 |
13.4 |
|
No Failure Found |
17 |
12.0 |
|
Engine Mount Pad
Cracked |
5 |
3.5 |
|
Cylinder Holddown
Bolts Broken |
4 |
2.8 |
|
Cam Drive Gear Failure |
4 |
2.8 |
|
Linkrod Failure |
4 |
2.8 |
|
Exhaust Manifold
Failure |
3 |
2.1 |
|
Turbo Failure |
3 |
2.1 |
|
Foreign Object Damage |
2 |
1.4 |
|
Scored Cylinders |
3 |
2.1 |
|
Hydraulic Lock |
2 |
1.4 |
|
Overspeed |
2 |
1.4 |
|
Overboost |
2 |
1.4 |
|
Nose Case Chaffed |
1 |
0.7 |
|
Nose Case Oil Leak |
1 |
0.7 |
|
Tappet Roller Pin |
1 |
0.7 |
|
Access Case Attach
Studs |
1 |
0.7 |
|
Magneto Case Cracked |
1 |
0.7 |
|
Master Rod Broken |
1 |
0.7 |
|
Oil Scavenge Pump Body
Broken |
1 |
0.7 |
|
Exhaust Guides Worn |
1 |
0.7 |
|
Low Power |
1 |
0.7 |
|
ANG C-97 ACTIVITIES |
Base Rating |
12 Month
Average |
Jan-Mar 1966
Avg. Eng. Life 983 |
Oct-Dec 1965
Avg. Eng. Life 950 |
Jul-Sep 1965
Avg. Eng. Life 975 |
Apr-Jun 1965
Avg. Eng. Life 958 |
|
Tulsa, Oklahoma |
5 |
1225 |
1182 |
1291 |
929 |
1500 |
|
St. Joseph, Missouri |
3 |
1245 |
1182 |
1272 |
1187 |
1340 |
|
Manchester, New Hampshire |
4 |
1237 |
1500 |
1200 |
1077 |
1174 |
|
Nashville, Tennessee |
2 |
1275 |
1383 |
1248 |
1167 |
1302 |
|
Phoenix, Arizona |
13 |
1011 |
950 |
1138 |
1068 |
890 |
|
Will Rogers, Oklahoma |
7 |
1160 |
1182 |
1344 |
1124 |
990 |
|
Salt Lake City, Utah |
1 |
1287 |
1500 |
1089 |
1162 |
1398 |
|
Memphis, Tennessee |
8 |
1149 |
1064 |
1189 |
1303 |
1041 |
|
Brooklyn, New York. |
15 |
961 |
1033 |
758 |
1003 |
1252 |
|
Philadelphia, Pennsylvania |
9 |
1149 |
872 |
1200 |
1500 |
1025 |
|
Savannah, Georgia |
10 |
1140 |
1118 |
1104 |
1262 |
1079 |
|
Minneapolis, Minnesota |
16 |
875 |
1100 |
774 |
745 |
882 |
|
White Plains, New York |
11 |
1077 |
1272 |
858 |
1292 |
888 |
|
Schenectady, New York |
6 |
1199 |
1219 |
1310 |
1040 |
1229 |
|
Wilmington, Delaware |
12 |
1050 |
950 |
1001 |
1500 |
750 |
|
Marietta, Georgia |
14 |
997 |
1037 |
1085 |
817 |
1049 |
|
Van Nuys, California |
17 |
793 |
696 |
781 |
825 |
870 |
|
ANG KC-97 ACTIVITIES |
Base
Rating |
12 Month
Average |
Jan-Mar 1966
Avg. Eng. Life 902 |
Oct-Dec 1965
Avg. Eng. Life 789 |
Jul-Sep 1965
Avg. Eng. Life 741 |
Apr-Jun 1965
Avg. Eng. Life 700 |
|
Chicago, Illinois |
5 |
848 |
797 |
1115 |
748 |
733 |
|
Milwaukee, Wisconsin |
2 |
1016 |
732 |
886 |
1500 |
946 |
|
Knoxville, Tennessee |
1 |
1171 |
1500 |
1500 |
902 |
782 |
|
Dallas, Texas |
3 |
1000 |
1500 |
1021 |
496 |
986 |
|
Wilmington, Ohio |
4 |
870 |
1500 |
593 |
892 |
496 |
|
MAC HU-97 |
Base
Rating |
12 Month
Average |
Jan-Mar 1966
Avg. Eng. Life 983 |
Oct-Dec 1965
Avg. Eng. Life 950 |
Jul-Sep 1965
Avg. Eng. Life 975 |
Apr-Jun 1965
Avg. Eng. Life 958 |
|
Wheelus |
2 |
1030 |
973 |
1310 |
847 |
990 |
|
Hickam |
1 |
1100 |
1131 |
1042 |
1033 |
1196 |
|
Burmuda |
3 |
936 |
934 |
891 |
860 |
1061 |

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